Thursday, February 19, 2015

Never Fails

 Note:  For further info on the Espar heater see the archive at right.

This past week has been very cold with sub-freezing highs and single digit lows.  Most daytime temperatures have been in the teens.  Yeah, pretty cold for our part of the country.  Normally this is not a big deal since we only have to deal with it when running between the boat and the car.  This being our final cold winter for many years to come we thought it would be no big deal.
 We've had our diesel heater for four winters now.  I calculated that amounts to about 9300 hours of usage with only minor maintenance such as replacing the glow plug and diffuser every year and the fuel pump once.  That's pretty good.  It's not an inexpensive way to heat your boat but it does keep it comfortable and it is fairly reliable.

This past weekend that reliability thing caught up to us.  I guess with 9300 hours I should have been expecting something.  Just as the temperatures dropped into the teens our heater no longer could keep up and temperatures inside dropped into the 60's even though the thermostat was set for 70.  At first I thought it was just because it was extremely cold outside.  Then I discovered strange sounds coming from the heater.  At first it sounded like a baseball card in your bicycles spokes.  It progressively got worse and developed into vibrations with the heater cutting out, usually in the middle of the night.

After a few days of this  I climbed down into the cockpit locker and did some maintenance on the heater.  I was pretty sure the problem was in the blower that supplies fresh air for the combustion process as well as the recirculated air that gets reheated.  The error codes displayed on the controller included #32, "blower motor short circuit".  The troubleshooting manual (click here) suggests a blockage in the fan.  I removed the input air duct and vacuumed it out.  I also used a paint brush and the vacuum to clean the fan blades.  I was kinda disappointed not to find any large dust bunnies in there.  As I was putting things back together I discovered the output air duct had popped off and was hanging down about a quarter inch, allowing cold air to be sucked in.  Yes!  That would explain why the heater couldn't keep up.  Not.

I fired up the heater and it seemed to run very nicely for a while but after a few hours it started making noises again and eventually stopped running.  It never seems to fail....bad things happen at the worst possible time.  At this point our weather had really deteriorated with a major snowstorm predicted for that night.  Temperatures were supposed to go below zero at some point too.  Inside the boat we'd be waking up to temperatures in the high 40's and 50's and that was because we were running two electric heaters to keep it from going any lower.

The next day I removed the heater and brought it down below for some major surgery.  After pulling off the intake hood I spun the fan.  It was locked up and after it broke loose I could feel resistance when I turned it.  OK, this is definitely the problem.  To remove the blower assembly I had to first remove the upper jacket shell and shell holder.  The manual says the blower isn't serviceable and is simply replaced as a whole unit.  The cost of this thing is about $700 so I wanted to play with it, break it down as much as I could.  I can see why it isn't serviceable.  Once you get down to the motor you still have the whole combustion side of the blower attached and it doesn't break down much beyond that.

I tried buying my replacement parts from the local distributor but they were closed because of the snowstorm that had blown through the night before.  I ended up going on-line and buying my parts from Lubrication Specialists (click here) located in Greenfield, Indiana.  I've bought parts from these guys before and their prices are excellent and delivery is speedy.  This time I asked for overnight delivery which added $86 to the bill.  Well worth it considering the temperature on the boat this morning was 49 degrees.  I also ordered a new injector and two new diffuser screens.

The parts arrived the next day at 1100, delivered to the marina office.  When I went to pick it up I climbed the stairs to the second floor office and from there I could look out across the Chesapeake Bay.  From up there I was able to see all the way across to the Eastern Shore and into the mouth of the Choptank River.  The Bay was frozen solid all the way across except for the shipping channel.  This is the first time I've seen this but it's not that uncommon.  Sharps Island Light at the Choptank River entrance has an interesting history (click here) of being damaged by ice on the Bay.

Although this could be considered a major repair for this thing the actual job itself is not difficult.  Once I had the parts unpacked it only took me about an hour to reassemble the unit and I took my time, cleaning as I went.  The Espar heater is really well built with a tight, compact design.  Parts fit together well and the only drawback for me was the need to invest in a set of star drivers.  This was the first time I've had to remove the cover and do major surgery but now that's it's done I'll have no fear if I ever have to go back in again.  There are few serviceable parts and all components are pretty easily accessible.

Once I had it back together and reinstalled in the cockpit locker it fired up on the second try and has run well ever since.  Just in time too because the weather went from bad to worse with temperatures dropping even further for the next three days.  Yikes!  That was close.

Monday, September 29, 2014

Espar D5 Repairs




Note: For installation information click here


Airtronic L "Troubleshooting and Repair Instructions"
Airtronic L "Installation, Operation and Maintenance"
Airtronic D2D4 Basic Repair Analysis
Airtronic Marine Installations
Espar Digi Controller Manual


With one more winter to contend with we want to make sure our diesel heater is going to be ready.  Over the last two winters we've averaged something like 2500 hours of non-stop running between December and early March.  Last year just as we were going to shut it down with the onset of warmer weather it decided to quit on it's own.  I let it go because it was no longer a high priority item and I had plenty of other stuff to work on.  As August rolled by I realized that time was getting away from me and decided to put the heater back up at the top of my priority list.

I did some preliminary troubleshooting and narrowed the problem down to the fuel metering pump.  It has a screen filter on the inlet and that was totally plugged.  I tried to clean it but punched a hole through the screen in the process.  That did give me better fuel flow but I still had errors and the heater wouldn't run for more than a few minutes.  I priced a new pump through our local supplier and they quoted me $300.  Uhm, sorry, but this little thing is not worth that kind of money.

This is a simple little piston driven pump, nothing complicated.  I saw the same pump priced on-line for $165.  I sincerely believe in supporting the local dudes but this was just ridiculous.  Even at $165 this thing is way over priced.  I shelved the project for a few weeks and gave it some thought.  This past weekend I opened up the manual and did some proper troubleshooting.  Following the error codes I came to the same conclusion, that the pump was bad, but I learned a lot about the system in the process.

Our D5 heater came with a small four button "digi controller".  To get the error codes you have to hold the top two buttons down simultaneously for about three seconds.  It'll then continuously cycle through all the codes in it's memory.  For this problem it showed #11 (under voltage cutout), #13 (flame sensor over temp), #48 (metering pump interruption), and #52 (safety time exceeded).  Espar has an excellent troubleshooting guide (Airtronic L Troubleshooting and Repair Instructions) which explains what to do for each code.  For code #11 I disconnected the main wiring harness connector "S1/B1" and put a volt meter across pins 1 and 10 where I saw 13.2 volts, just as it should be.  For #13 it suggests checking the combination sensor (flame and over temp) but it goes on to mention fuel quantity too and this ties in with the other codes so I moved on to the next one, #48.  This says to check the resistance across the two leads on the fuel metering pump.  It's supposed to read 9.5 ohms but mine reads 0.2.  I also noticed that code #47 suggests that if you have error code #48 then just go ahead and replace the fuel metering pump.  OK, I'll do that.  In another manual (Airtronic D2D4 Basic Repair Analysis) it mentions that the most common cause of metering pump failures is extended periods of non-use causing the piston to freeze.  I suspect this then causes the coil to short out and give the indication I see here.  We don't run the heater from March to December, pretty much nine or ten months straight.  I think that qualifies for "extended periods".  #52 is just a safety feature built into the program that only allows the heater to be in the start-up mode for a short period of time.  If it doesn't go into run mode within that time it switches over to shut-down mode to keep itself from turning into a lump of molten metal.  I went ahead and ordered the $165 metering pump on line.  It's worth mentioning that the screen for the pump is available separately at a fairly reasonable price.  If you don't have an in-line filter upstream from the pump then it might be worthwhile investing in a few of these.

Espar provides some very nice information in these two manuals.  The "Basic Repair Analysis" is intended for other similar models but has color photos and good explanations of what caused specific problems.  The other one, "Troubleshooting and Repair Instructions", steps you through the troubleshooting procedure and provides drawings and schematics.  I've got both of these in PDF form on my iPad along with most manuals for all our gear on board.  Another nice one to hold onto is the installation manual that came with the original kit.  This provides a nice electrical diagram with color coding for all the wires.  I've attached all three of these, and more, at the top of this post for anyone who might be interested.

Monday, December 27, 2010

Espar Diesel Heater D5 Installation

Last winter we had a reverse cycle heating and air conditioning system installed by the good folks up in Gratitude.  At the time we were thinking more about A/C than heat because we hadn't even considered living aboard full time yet.  Now that La Vida Dulce is the place we call home things are viewed from a different perspective.  We've been very aware of the approaching winter and are doing everything we can to ensure we'll be toasty warm and cozy when it's 20 below outside.  The main focus is heat (duh).  The reverse cycle system uses the water we're floating in to make hot or cold air.  It's only good as long as the water temperature is above 38 degrees F.  Usually by January it has dipped down into the 30's or completely frozen over.  We could use electric space heaters but the power at the dock has a reputation for being shut off periodically through the winter and it's limited to 30 amps so we're gonna need something else.

Espar makes a series of forced air and hot water diesel heaters.  Check out this video on how the forced air heater works (click here).  We chose a kit that includes a D5 forced air heater with enough ducting, fittings, vents and hardware to complete a system for a 45' boat.  When we went to pick it up from Annapolis Cruisair (web site) we found a huge box on a pallet that would barely fit into our Ford Escape mini SUV. Once we got it down to the boat we found a very complete system but very poor installation instructions.  I suppose this is because each install is unique but there could be more info on common things like what size holes to cut for the duct work and suggestions for mounting the heater.  I guess these kits are really meant for professional installers.  Looking on the Espar website for some ideas, I found a video on how to install this thing.....in a tractor trailer.  Apparently these are used mostly by truckers to keep their berths toasty when they stop for the night, saving fuel by not running the engine the whole time.

I read through the book which was mostly about government regulations in Germany, safety concerns and hazards of working with electricity and about diesel fed fires.  OK, so I'm not going to get much help on this project.  I decided to be really organized and plan everything out ahead before I started cutting holes in the beautiful teak cabinetry.  It appeared that the best route for the duct-work would be through the cabinets on the port side.  I wanted to mount the heater in the cockpit locker and run the duct under the aft cabin bunk, jump over to the cabinets and then run forward from there.  Cheri didn't like the idea of the duct showing where it poked out of the bunk and I told her it would be boxed in so it wouldn't show.  She asked how many years would go by before I got around to boxing it in.  OK, plan B.

I looked into running the duct down the starboard side.  We'd lose the ability to heat the forward head going this way but we figured we could live with that.  I spent an entire day crawling around the boat before I nixed the idea of running the duct down the starboard side.  The refrigerator's location makes it pretty much impossible to run any ducting down that side without having too many tight bends and taking up too much storage.

Plan C.  I spent another two days emptying out cabinets and crawling around under the cockpit before I settled on a definite plan.  I'd attach a plywood shelf to the inside of the hull in the port side cockpit locker.  The heater will be mounted there and the supply side duct-work would go through the bulkhead into the aft cabin coming in just under the shelf above the bunk (This will have to be boxed in but will make the shelf deeper and more usable.  The idea of running the duct under the bunk was nixed because of tight bends required and space issues).  From under there the duct enters the aft stateroom cabinet and hanging locker, goes through the bulkhead into the aft head and continues through cabinets all the way to the forward head.

I'm using a 4" hole saw for the 90mm duct and a 3.25" hole saw for the 75mm duct.  There will be four vents; aft stateroom at the base of the hanging locker, main salon at the base of the settee, forward stateroom at the base of the hanging locker and forward head low on the bulkhead next to the sink.  Where each vent branches off from the 90mm duct there is a "Y" and the vent line is reduced to 75mm duct.  This makes it nice for snaking the vent lines and the larger main duct can be kept higher up in the cabinet towards the back and out of the way.

The heater uses a 90mm return line that will be run from the galley at the base of the refrigerator.  This should help to circulate the air throughout the boat without having to run additional vent lines.  The thermostat / control will be mounted at the Nav Station.  Each of the vents are fully adjustable and can be closed down to adjust the flow and rotated to adjust direction.  Pretty nice.

OK, so after I scoped out the location for the duct I began cutting holes and running the primary duct.  Once this was in I sat down and read the manual again.  I somehow missed the part where it explains how to plan the duct work.  Espar has assigned a numerical value to every component.  90mm duct is given a number based on it's size and length.  A 90 degree bend has a value.  Reducers have a value.  Vents have a value.  The heater itself is given a value of 10 and you're supposed to add up everything else in the primary, secondary, and return lines and keep the total under 10.  This is because restrictions in the ducts accumulate and create a backup at the heater, which, in turn, creates excessive heat buildup.  I went through my design and found it's total to be 14.75.  That's not gonna work.  I re-thought what I had, made some changes to the parts that hadn't been installed yet, redirected one section and came up with 8.0.

Originally I had all four vent lines (secondary) being reduced at the "Y" to 75mm and running to a closeable vent.  The biggest change I made in the design was having the primary run with 90mm duct all the way to the Main Salon where it ends with an open vent with a metal grid over it.  I suppose the grid is to keep Bella out of the ductwork (I wonder what kind of rating they'd give her!).  According to the book, for my calculations I can ignore the other three secondary lines because they can be considered closed.  When they're open they reduce back pressure even more, which is a good thing, but with just the primary line running we're now in a safe pressure zone.

With this taken care of I ran the rest of the ductwork over the weekend of 12/4.  I also changed the outlet location in the forward head once I got the ductwork up that far and realized my original plan wouldn't work.  With this project ya gotta be flexible.  I ended up running it through the wall behind the sink and exiting the cabinet just under the shelf behind the toilet.  With the supply ductwork installed the worst part of the installation is over but I still have a lot to do.  There's a return duct to put in, which'll run either to the Galley or the aft cabin, haven't made up my mind on that just yet.  Also have the fuel line to run from the tank to the heater.  And there's the control and power wiring between the Nav Station and the heater.  And then there's the exhaust hose which requires a hole to be cut in the transom.  Also need a fresh air intake for combustion.  Oh yeah, there's also a drain line to the bilge from the heater.  Hmmmm.  I guess I still have a bit to do here.

12/12.  I spent all day Friday and Saturday working on mounting the heater in the cockpit locker.  The plan was to build a plywood shelf  that it could be bolted to and attach that to the inside of the hull.  This would put the heater in a good position to attach the supply and return ducts and give plenty of room for everything.  Good plan.  I formed up a mock-up for the shelf out of cardboard and duct tape and spent a lot of time matching the curvature of the hull.  This was important because I planned to attach it using 3M 5500 and then glassing it in for additional support.  Once I had the cardboard form to my liking I copied it onto some plywood, cut it out on the dock using my new handy dandy saber saw, and then mounted it with duct tape to check out my work.  Not even close.  It was way out of level for one thing and seeing it in action made me realize that this just wasn't going to be strong enough to hold that heater.  The heater weighs about 25 pounds and I pictured it breaking loose in a heavy chop out in the middle of the Bay.  Plan D.  I moved the mounting location to a plywood bulkhead which places the heater "port and starboard" instead of "fore and aft".  It also adds some bends in the duct work.  I think I'm still in the "safe" zone with my math calculations though and I feel the mount is way stronger.

The following Tuesday while I was at work I realized that progress on this project was going way too slow so I took Wednesday and Thursday off to try to wrap it up before the really bad weather hit.  That night the really bad weather hit.  At 0400 I woke up to find the cabin temperature was down to 56 degrees.  The reverse cycle system had called it quits because the water temperature had fallen below 38 degrees.  The heat exchanger looked like a block of ice.  I think I musta had a vision when I took that time off.  As soon as I realized there was no chance of getting the heat exchanger going I got to work on the diesel system.

The first thing I did was cut holes in the bulkheads for the return air duct.  I hadn't really planned this part out until now so I kept it easy and ran it to a high spot on the aft bulkhead of the aft cabin.  This will draw the air back through the boat and hopefully help to heat this section of the room at the same time.  It's also the easiest way to run the duct.  I had originally wanted to run it under the reefer in the galley because it would have helped to evenly distribute the heat to the other side of the boat.  This option would have required way too much effort and I just didn't have the time for that now.  Easy is good.  So I got the return duct hooked up and while I was in the cockpit locker I also ran the combustion supply and exhaust lines and wrapped the last with braided fiberglass mat as an insulator.  The exhaust line can get smokin' hot so it's a good idea to protect everything around it from melting down.  Once I got this done Cheri and I ran the fuel line.  The kit comes with a coil of copper tubing to be used for this but I found it to be about 10' short so we went out and bought a 50' roll.  We ran it under the cabin sole from the fuel tank, past the engine, out through the generator compartment under the cockpit and into the locker.  Here it connects to the fuel pump and then runs up to the heater.  The fuel pump needs to be mounted at an upward angle between 15 and 35 degrees to keep air pockets from forming which would kill the fuel pressure.  For the connection at the tank end we used a special fitting at the top of the fuel tank and ran the riser tube down through that, cutting off the bottom at a 45 degree angle so it sits about 2" off the bottom.  That'll help to keep tank grunge out of the line.

With the fuel taken care of it was time to run the power and control lines.  The kit comes with a nice bundle of wire that's connected at one end to the heater through a pre-assembled multi-pin connector.  From there it branches off into three bundles; fuel pump, power and ground, and a 6 wire bundle to be connected to the thermostat/control.  All of these required adding connectors of one type or another.  The fuel pump and power went fine.  By the time I started in on the thermostat line it was 2000 (8pm) and I was getting pretty tired.  This line uses a six pin connector that requires adding pins to #18 wire and inserting them into a two piece connector.  Once the pins are in they have these little prongs that pop out on either side to hold it in place.  I'm sure there's a special tool that costs $150 to use for these pins.  Using a cheapo wire stripper doesn't cut it because the pins are so small that it's hard to get a good crimp on them.  I ended up not using the connectors and just soldered and shrink wrapped the wires.

Update:   I later needed to remove the thermostat control from the Nav Station and had to cut the wire to get it out.  To reinstall it I used Deutsch connectors (click here) and was so impressed with the quality I've continued to use them in other parts of the boat.  The best example of this is at the mast where a large number of wires need to be disconnected for unstepping the mast.

With the control line connected we fired up the system.  This took three attempts before it finally fired because it takes a while for the system to draw fuel through the line.  Once it fired though, we had heat.  Woohooo!

We did run into a few problems afterwards.   The system kept shutting down and didn't provide any error codes.  It would reset OK but would run for half the day then shut off again.  We eventually found out that the factory preset is for a ten hour operation.  I'm sure this is a safety thing for when the heater is installed in a truck.  Not what we need in a boat though.  To reset this you have to go into the program and reset it for continuous operation (click here and scroll to page # 11).  This isn't mentioned in the users manual and we only found out about it by going to Annapolis Cruisair for help.  A second problem showed up after the system had been in operation for about a week.  It stopped running, gave an error code of 13, would manually reset again and then only run for about 15 minutes before quitting.  The owners manual only gives four error codes and this isn't one of them.  We called Bryan at Annapolis Cruisair on Christmas Eve and he wasn't familiar with this code.  He spent a good portion of his day getting in touch with a factory tech and finding out what this meant.  Turns out the problem is with the airflow being restricted and causing hot spots in the heater.  There are two internal sensors that compare temperatures and if there's too much variation they shut the system down.  The tech said we probably have some really tight bends in our ducts.  Gee, he was right.  The return line that I put in during the mad rush to get the system running was the culprit.  I removed the duct from the heater and let it run open for three days and never had another problem.  Of course now I've got a system that needs to have the cockpit locker open when it runs so it doesn't suck bilge air into the Main Salon.  Next week I'll work on rerouting the return duct so it doesn't have any restrictions.

Update:  I ended up running the return duct from the starboard side of the aft bulkhead in the aft cabin into the starboard cockpit locker.  It runs beneath one exhaust hose and then circles around behind the cockpit into the port side locker.  There I re-mounted the heater unit on the inside of the hull so that both ducts, supply and return, both have a more direct run with no sharp turns.  The mount for the heater is made from 3/4" plywood and is epoxied to the inside of the hull.  The 2 part epoxy I used is from West Marine and includes a filler so when you squeeze it out and mix it up it's thicker so it won't tend to run out so easily when you goop it into place.  Never-the-less, I used masking tape to hold it in place for two days until it dried.  For the best explanation of my shelf style bracket see the drawing on the left.

So I learned that the Espar number planning game is real and you really do have to stay within the limit set for your heater.  In our case this was 10.  When I scrambled to finish the system I cheated and added too much restriction.  Overall, I'm really impressed with this do-it-yourself kit from Espar.  The instructions are kinda lousy but the system is simple enough that it's not too tough to figure out for yourself.  The actual installation is pretty involved but the worst part is unloading all those cabinets and cutting holes in that beautiful teak.  Once you get started it goes pretty quickly.  You just have to spend the time in the beginning planning it all out.

I also want to say that I'm impressed with the people at Annapolis Cruisair and Espar.  I called Bryan on his cell phone and interrupted his personal time with his family on Christmas Eve.  He was very gracious and went out of his way to get us an answer to our problem.  He contacted the Espar tech at his home and worked with him to figure out the problem.  Bryan then called me back and offered several possible solutions but felt the duct restriction was the best possibility.  All this on Christmas Eve!  These guys sell a quality system and provide unbelievable support.  Highly recommended.